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Teaching a new guy about turbo sounds led to a shop-wide debate
Honestly, back when I started working on diesels, we relied on ear and experience more than tech. Tbh, this led to some funny misunderstandings. I recall a customer who was convinced his 'turbo whistle' was a leak, but it was just the normal sound. We had a whole debate in the shop about it, and it turned into a teaching moment for the new guys. Ngl, nowadays with diagnostic tools, you'd just scan it and know, but back then, it was all about hands-on problem solving. That social interaction, even when awkward, really connected us. I kinda miss those days when fixes weren't just a click away.
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taylor_wells2d ago
Man, that really hits home. Back then, you had to use your ears and your know-how, not just a computer screen. Those shop debates built a real connection between everyone working there. Fixing things felt like a team effort, with all the talking and laughing along the way. Now everything is so quiet and quick with diagnostics, but it loses that personal touch. Your story about the turbo whistle debate is exactly the kind of thing that made the job mean more.
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matthewl671d ago
But isn't there still room for those debates even with diagnostics? I've seen guys argue over computer readings just as much as over a turbo whistle. Maybe @taylor_wells, the team feeling comes from how we work together, not just the tools.
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patricia_hill602d ago
Yeah that "team effort" thing @taylor_wells mentioned is so true. Those debates weren't just about fixing the truck, they were how the new guys really learned why things worked. That kind of lesson stuck with you way more than a fault code, lol, even if it was louder and messier.
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eric_gonzalez261d ago
Ever notice how a sound can mean two totally different things on two different engines? I had a Cummins ISX with a high-pitched whine everyone swore was a failing turbo bearing, but it was actually just a harmonic from the aftercooler pipe being a fraction too close to the bracket. We tore into that turbo for nothing, and the fix was just loosening a clamp and shifting the pipe a quarter inch. It was one of those things you only learn by getting it wrong first.
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